Hi guys, hope you all had a nice summer!
My car was today at one repair shop, but they didn't find the reason why wgdc is what it is: it is still as before.
Car was also on dyno with base 98 tune, and yielded only
156Kw's/300nm torque

That tune in my car actually felt really mild on butt dyno, and they said also that there was a total lack of power on high rpm's.
They mechanically metered boost and couldn't get anything over 0.7-0.9 bar up to 6600rpm (messing with actuator arm and bcs hoses way they could get 1,5), so
i'm really puzzled now. Any idea why Versatuner was showing high boost, is there something wrong with MAP sensor etc? If logs attached don't show too high boost anymore, then it might was the Actuator arm that was rubbing to the heat shield? I carved some off from heatshield and now it's ok what comes to rod movement. The dynoing btw was done without the heat shield, so there weren't any obstacles.
Well, tonight I returned the car back to stock and it was totally different, at least acceleration was hugely better. I haven't dynoed with stock tune yet because it's
80euros/shot, but that could be a good idea (to see if my butt dyno is accurate

).
Do you have any idea why base tune is performing as it is?
